markind
Posts: 300
Joined: 11/11/2006 From: San Jose,
CA, USA Status: offline
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Totally SOLO Today! Flight Report for Saturday morning 12-1-07. Conditions: Cold and calm. A little rain came through and went forcing one 15 minute break time. My son had other commitments, and I was all alone at the flying field today. Felt like my own personal airstrip. Yeah baby. Flew my Multiplex MiniMag around first, to calm my nerves. After a perfect landing, I started F-22 Raptor Flight Prep Ops. Got everything together, so I began working with the engine. I tried working the 'Miracle Plug', which is an 'RC Long' plug as is supposed to be good for all 4 and 2 stroke engines. No idle bar. After a lot of trials and tweaking, I still could not get a reliable idle and transistion to WOT. So I went for another plug, very similar but I am guessing a bit hotter-running. Better! Still a bit rough, but she passed all the tests on the ground, and I gave her clearance for flight ops. One stall on takeoff (just before takeoff actually - she hadn't even got rolling yet), and 3 perfect takeoffs. 3 decent landings, but ALL of them were Off The Runway! The last landing was best, as I had increased the flaps a bit to a full 1" down. She rolled into the rough instead of bouncing there like on the first two tries. Ugh, not pretty, but NO DAMAGE!! The landing gear still seems straight (I will look at it more closely later) and the wingtips never touched dirt. Surprising, since the motor kept getting stopped by the nose bouncing down into old dry cow turds... I still have a lot of fresh 10% airplane fuel left, so I need to figure out how to get her running smooth again like before the stock plug burned out. I learned a lot today and figured out a few things about engine start-up, and I did several starts 'by hand' (no chicken stick!) today. I did not concentrate on the actual flights themselves, but I did have good time with a bunch of loops and rolls. I was mainly focused on trying to get the landings better. Twice I came in, bounced high, and then aborted the landing with WOT. Thats my first two Touch And Go's but completely unintentional. Cleanup took a long time - oil and dirt all over. Yuck. Lots of Windex dispensed. Overall, pretty good for being totally alone. Its much better to have some company but today I HAD TO FLY!
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