Maloney 100 problem
#1
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From: McMinnville,
TN
Ok
I have a Moloney 100 on a kit built Taube. I have pulled my hair out over a glitch problem. The plane has no problem while the engine is not runnig, but as soon as I get a few feet she starts glitching. I have checked just about everything I can think of and it still will glitch. It is a gas engine and has the old style magneto ignition. I think the only way to stop this is to change the ignition to cdi, but I hate to spend the extra $ if it is something else. Please help?
I have a Moloney 100 on a kit built Taube. I have pulled my hair out over a glitch problem. The plane has no problem while the engine is not runnig, but as soon as I get a few feet she starts glitching. I have checked just about everything I can think of and it still will glitch. It is a gas engine and has the old style magneto ignition. I think the only way to stop this is to change the ignition to cdi, but I hate to spend the extra $ if it is something else. Please help?
#3
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From: Coalmont,
TN
It has the old type that came with it and it is around 20 years old I am sure because that is how long it has been out of production. I think you may have got the fix. I am not sure what size and type it may need. I have a Zonah 26. I will see if they are the same. Thanks!!! I will report.
#4
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The threads on the Champion RZ7C plug in the G26 are too long, the piston might hit the side electrode...The CM6 plug in the engine is not a resistor and there are no short resistor plugs..
A fix would be a shielded cap from C&H, DA, or 3W that fits the plug, but the mag might not be strong enough to fire a resistor plug, and the shielded caps have a built in resistor...
Or you might get by with a spacer under the resistor plug if the mag wire is long enough...
A CDI ignition would save much weight and would work, but the cost might be more than you want to pay....
You might try a new CM6 and aluminum foil around the plug and wire, all the way back to the mag coil...Secure it with some tie wraps...
A fix would be a shielded cap from C&H, DA, or 3W that fits the plug, but the mag might not be strong enough to fire a resistor plug, and the shielded caps have a built in resistor...
Or you might get by with a spacer under the resistor plug if the mag wire is long enough...
A CDI ignition would save much weight and would work, but the cost might be more than you want to pay....
You might try a new CM6 and aluminum foil around the plug and wire, all the way back to the mag coil...Secure it with some tie wraps...
#5
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From: Coalmont,
TN
RCIGN1, I can tell you know what you are talking about. The engine in not worth the $ money to put a new ignition on, so a plug or cap. I did try another cm-6 plug with the same luck. I called NGk. they make a resistor plug that is only 1 mm longer. It is the NGK cmr6a stock number 1223. if I have the room it should be fine if not I will add a 1mm shime and it should still be fine. I hope this fix's the problem. If not DA makes a cap that may work too. I will report. Thanks for all the info.
#6
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Go to www.sparkplugs.com, check out the differences between the CM6 and the CMR6...The thread is way longer on the bottom and the insulator is way longer on top...
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From: Coalmont,
TN
NGK stated it was only 1mm longer in length. It would most likely work, but they would not recomend it. I think the plug is $3.19. might be a waste of time, but I will try it and hope[
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#8
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From: Coalmont,
TN
OK The plug stoped the problem, but this is the worst engine I have ever had. It is heavy, low power, and is hard to start and run smooth. I got it at a deal and hoped but. I should have know it was a bad one because they have not made it in years. replaceing it with a Zenoah 23 I have.
Thanks
Freebird
Thanks
Freebird




